"state_well_number","group_number","remarks_1","remarks_2" 3401901,1,"Well # 28 in M-223. ", 3402702,1,"Oil test. Log Q-5. ", 3402801,1,"Oil Test. Log Q-2. ", 3402901,1,"Oil test. Log Q-7. ", 3403101,1,"Observation well. ","Reported dependable supply. " 3403303,1,"Reported yield 51 GPM with 99 feet ","drawdown after 36 hoursa in 1972. " 3403303,2,"Specific capacity 0.5 GPM/ft. ", 3403501,1,"Drilled for rig supply. Base of ","Wilcox at 225 ft. Jetted 60 gpm " 3403501,2,"with 50 feet drawdown after 2 hours","Aug. 22, 1966. " 3403502,1,"Oil test. Base of Wilcox at 188 ","feet. Log Q-16. " 3403503,1,"Owners well #5. Reported yield 100 ","GPM with 125 feet drawdown after " 3403503,2,"pumping 24 hours in 1983. Specific","capacity 0.8 GPM/ft. Aquifer test " 3403503,3,"data in TWDB files. ", 3403505,1,"Owners Spinks #10 well. PWS ID ","#2500015O. " 3403605,1,"Owners Lynn #9 well. PWS ID ","#2500015N. " 3403702,1,"Drilled for rig supply. ", 3403702,2,"Jetted 50 gpm with 60 feet drawdown","after 3 hours on Mar 19, 1968. " 3403704,1,"Observation well. Supplies house ","and about 100 head of hogs. " 3403802,1,"Estimated flow of 125 gpm in 1969. ","Well on N. side of Lake Fork Creek." 3403806,1,"Reported yield 100 GPM with 85 feet","drawdown pumping 36 hours in 1985. " 3403806,2,"Specific capacity 1.17 GPM/ft. ", 3403807,1,"Reported yield 58 gpm with 78 feet ","drawdown pumping 24 hours in 1984. " 3403807,2,"Gravel packed from 364 ft to 408ft.","Cemented from 0 to 364 ft. " 3403807,3,"Deep(east) well at Hogansville ","plant. " 3403808,1,"Reported yield of 15 gpm in 1980. ", 3410202,1,"Observation well. Water smells of ","hydrogen sulfide. " 3410301,1,"Old City Well No. 1. Test hole ","drilled to 555 ft. Base of Wilcox " 3410301,2,"at 207 ft. Plugged back to 213 ft.","Abandoned and replaced by 3410302. " 3410301,3,"Reported yield 275 gpm with 79 feet","drawdown pumping 24 hours in 1950. " 3410302,1,"City well No. 2. Test hole ","drilled to 305 ft. Base of Wilcox " 3410302,2,"212 ft. Plugged back to 212 ft. ","Set 212 ft. of 6 in. casing. " 3410601,1,"Water not used for drinking. ", 3410602,1,"Supplies Dunbar Gas-processing ","Plant. Base of Wilcox at 150 ft. " 3410602,2,"Pumping test by Layne-Texas Co., ","March 25-26, 1966; drawdown of 51.5" 3410602,3,"ft. discharging an average of 21 ","gpm for 24 hrs. Plant closed 1969." 3410602,4,"Aquifer test results in TWDB R-169.","Data in TWDB files. " 3411201,1,"Oil test. Base of Wilcox at 280 ","feet. Log Q-11. " 3411202,1,"Dug. Brick casing. Water high in ","iron and nitrate, not suitable for " 3411202,2,"human consumption. ", 3411203,1,"Supplied water for drilling oil ","test. Base of Wilcox at 305 feet. " 3411203,2,"Reported yield 60 gpm with 90 feet ","drawdown pumping 2 hours in 1967. " 3411205,1,"Reported yield 150 GPM with 192 ","feet drawdown after 24 hours in " 3411205,2,"1979. Specific capacity 0.78 GPM/- ","ft. " 3411206,1,"Owners well #3a. Reported yield 52 ","GPM with 67 feet drawdown after " 3411206,2,"pumping 36 hours in 1986. Specific ","capacuty 0.77 GPM/ft. " 3411207,1,"Owners well #4b. Reported yield 56 ","GPM with 101 feet drawdown after " 3411207,2,"pumping 36 hours in 1986. Specific ","capacity 0.55 GPM/ft. " 3411301,1,"Oil test. Log Q-10. ", 3411501,1,"Bored. Concrete tile to bottom. ","Reported water level declines " 3411501,2,"during dry periods but well has ","never failed. " 3411502,1,"Water not used for drinking, stains","plumbing. " 3411504,1,"Reported yield 45 GPM with 170 feet","drawdown after 36 hours in 1995. " 3411504,2,"Specific capacity 0.26 GPM/ft. ", 3411601,1,"Oil test. Base of Wilcox at 475 ","feet. Log Q-1. " 3411906,1,"Oil test. Base of Wilcox at 520 ","feet. Log Q-4. " 3419302,1,"Drilled to 640 ft. Plugged back ","and set 8 in. casing to 257 feet. " 3419302,2,"Tested at 45 gpm with 15 feet draw-","down in 1934. Flowing 8 to 10 gpm " 3419302,3,"on July 24, 1969. Well # 57 in ","M-223. "